2ndGenGuy
01-16-2009, 11:16 PM
Put my ES2 on the dyno for the last time. Over 310,000 miles on that good old engine. Still not running too bad. I managed to finally get that Weber 38 to work. It looks like since my original dyno, I've managed to squeeze a few extra HP.
My original dyno put down 67whp. That was with the ignition timing WAY off (probably a loss vs stock power), and only a 32/36 Weber, stock exhaust manifold, original flywheel. Also done on a Mustang dyno (which tends to read a little low) at about 80 degrees F with a decent amount of humidity.
I went home tonight, fixed all my vacuum leaks (which was originally why my Weber 38 wasn't running right). Re-jetted the carb on the butt dyno at home (spent about 20 minutes on it). And drove it into the shop. The 38 ran pretty damn good. It was running a little bit on the lean side at first. But not bad for tuning by ear and butt. Ran about 93hp on the first run with about a 17afr at idle and about 16 in the top end.
So after getting the AFR properly tuned using the shop's wideband, the second run came out much better. I got the AFR, still a bit lean, to about 15 across the board by just adjusting the idle mixture screws. Then it jumped up to a peak of 97.1whp.
Since the last dyno, I've been able to properly set my timing correctly. The old flywheel was caked in grease and I kinda went by ear, which was way off. I upgraded the 32/36 up to a 38. Installed some Accel 8mm plug wires and MSD coil. Installed my DC Sports header and had a full custom 2.25inch exhaust. The results are pretty amazing. Even if the old dyno read a bit low, I got a good jump in horsepower from all the work that's been done. It was also cold as fuck out and fairly dry.
There's probably a ton of little things I could have done to squeeze it up to 100hp, I'm pretty sure. Probably some minor porting on the intake manifold. Smooth out the transition between the adapter plates. Probably could have upped the jet main size by one size since the throttle linkage was only opening about 95% of the way. And when we manually opened it to full, it leaned out a bit more but didn't get any more HP. Also, cleaning the massive amounts of soot out of the chokes, removing the choke plates, in-setting the screws in the throttle plates for a bit better flow. But anyways, it was fun and I'm happy.
http://farm4.static.flickr.com/3120/3202511499_bf58a26f9e.jpg (http://www.flickr.com/photos/jgturk/3202511499/)
http://farm4.static.flickr.com/3405/3203368108_eb9471979d.jpg (http://www.flickr.com/photos/jgturk/3203368108/)
http://farm4.static.flickr.com/3354/3203368814_a1055a6dab.jpg (http://www.flickr.com/photos/jgturk/3203368814/)
http://farm4.static.flickr.com/3463/3202519347_4d6f0dc15d.jpg (http://www.flickr.com/photos/jgturk/3202519347/)
http://farm4.static.flickr.com/3443/3202520663_9944dc4c8b.jpg (http://www.flickr.com/photos/jgturk/3202520663/)
http://farm4.static.flickr.com/3393/3202522011_aedbfb6f6a.jpg (http://www.flickr.com/photos/jgturk/3202522011/)
And here's the video of the second and third runs. Fucking camera didn't have auto-leveling built in for the mic, so it clipped the shit out of the audio. Sorry for the awful noise.
http://www.youtube.com/watch?v=5iXgQ5N7Mwc
I'll definitely be putting the B20A up on this same dyno, so I can compare more accurately between the two engines.
:rockon:
Now to proceed with the B20A swap. :hsugh:
My original dyno put down 67whp. That was with the ignition timing WAY off (probably a loss vs stock power), and only a 32/36 Weber, stock exhaust manifold, original flywheel. Also done on a Mustang dyno (which tends to read a little low) at about 80 degrees F with a decent amount of humidity.
I went home tonight, fixed all my vacuum leaks (which was originally why my Weber 38 wasn't running right). Re-jetted the carb on the butt dyno at home (spent about 20 minutes on it). And drove it into the shop. The 38 ran pretty damn good. It was running a little bit on the lean side at first. But not bad for tuning by ear and butt. Ran about 93hp on the first run with about a 17afr at idle and about 16 in the top end.
So after getting the AFR properly tuned using the shop's wideband, the second run came out much better. I got the AFR, still a bit lean, to about 15 across the board by just adjusting the idle mixture screws. Then it jumped up to a peak of 97.1whp.
Since the last dyno, I've been able to properly set my timing correctly. The old flywheel was caked in grease and I kinda went by ear, which was way off. I upgraded the 32/36 up to a 38. Installed some Accel 8mm plug wires and MSD coil. Installed my DC Sports header and had a full custom 2.25inch exhaust. The results are pretty amazing. Even if the old dyno read a bit low, I got a good jump in horsepower from all the work that's been done. It was also cold as fuck out and fairly dry.
There's probably a ton of little things I could have done to squeeze it up to 100hp, I'm pretty sure. Probably some minor porting on the intake manifold. Smooth out the transition between the adapter plates. Probably could have upped the jet main size by one size since the throttle linkage was only opening about 95% of the way. And when we manually opened it to full, it leaned out a bit more but didn't get any more HP. Also, cleaning the massive amounts of soot out of the chokes, removing the choke plates, in-setting the screws in the throttle plates for a bit better flow. But anyways, it was fun and I'm happy.
http://farm4.static.flickr.com/3120/3202511499_bf58a26f9e.jpg (http://www.flickr.com/photos/jgturk/3202511499/)
http://farm4.static.flickr.com/3405/3203368108_eb9471979d.jpg (http://www.flickr.com/photos/jgturk/3203368108/)
http://farm4.static.flickr.com/3354/3203368814_a1055a6dab.jpg (http://www.flickr.com/photos/jgturk/3203368814/)
http://farm4.static.flickr.com/3463/3202519347_4d6f0dc15d.jpg (http://www.flickr.com/photos/jgturk/3202519347/)
http://farm4.static.flickr.com/3443/3202520663_9944dc4c8b.jpg (http://www.flickr.com/photos/jgturk/3202520663/)
http://farm4.static.flickr.com/3393/3202522011_aedbfb6f6a.jpg (http://www.flickr.com/photos/jgturk/3202522011/)
And here's the video of the second and third runs. Fucking camera didn't have auto-leveling built in for the mic, so it clipped the shit out of the audio. Sorry for the awful noise.
http://www.youtube.com/watch?v=5iXgQ5N7Mwc
I'll definitely be putting the B20A up on this same dyno, so I can compare more accurately between the two engines.
:rockon:
Now to proceed with the B20A swap. :hsugh: