Today's update:
So today I pulled in the hatch after shuffling all the car's in the driveway around.
After I warmed it up for a bit I did a compression test after I got it in the shop. Which was a difficult task by myself and with a dead battery(duh, I grabbed a working one).
It went #1 = 175, #2 = 175, #3 = 185, #4 = 183
I took multiple reading's of each cylinder and those were the highest. I also put a bit of oil in each cylinder after those readings and got higher reading's(around 190-200ish), so I don't think my ring's are the healthiest..The engine was also cooling down so I don't know if this affected my reading's along the way. It's still pretty healthy but I thought it would be better.
So I drained the fluids and took off the hood, these are more of a before picture:
Bye bye N/A, oh wait...
It look's as if I've been running on 3 cylinder's this whole time :O Talk about a fail... still managed to make 130whp though haha. So far I'm thinking it's a shitty injector, I will know more when I get around to tearing everything off.
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